So we had what I though was a failure with this beastie a week or two back. This would mean a pain trip back into the insides to see what may be wrong. To this end I have bought a spare RX and Cobra so that I can at least try to work out where the issue may be. However on undoing the beast I found a wire that had come out of a screw terminal. Now the issue was not this as this wire was from the Rx to the MLS card. So I tried the loco undressed as it were and all was well, so the problem is not resolved in that I have not a clue what was wrong, best guess is that the batteries in the TX were out of place a little and not giving full power. This was probably why the lamp on the Tx looked a little dark as when I removed the batts to check them they were a full 1.5v and the light was brighter when put back. Hm. Anyhow during this I noticed some cosmetics that needed attending to and it was considered worthwhile to get the MLS IR receiver into the cab rather than burried deep within the inards so that I can change the way that the sounds are working.
The IR and wires to the speaker go up the back of the Cab and had originally been glued in place however this all came loose so I used some very this insulated wire to hold it in place through a couple of holes in 2 places. Hopefully you can just manage to work the inside on the second picture, I reasoned that the IRR looked like some kind of junction box inside the cab. Not quite sure why Bertie is sideways. The outside wire will be hidden in some kind of plasticard trunking as seen in the final picture.
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Another thing that I am doing when any work gets sone to my Battery fleet is to make the Fuse accesible, again it is a pain to have to pull a loco to bits to get to the fuse. There was a bit of a pondering issue with this as the place for a tool box has cosmetic opening doors so as I had blocked them on the otherside I reasoned that I should not do the same this side. Thus this under footplate box was added the other side as well. The wires to the fuse needed to be extended to facilitate this so Mr.Soldering Iron was in action for that task. There is just enough space to get the fuse out with some gentle manipulation.
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Below can be seen that some of the handrails have suffered some damage, careful drilling into the ends with a very fine drill and some 47thou copper wire was Hafixed into the holes. I only want these to be press fit as this tends to save further damage as they will pop out with any abuse. The rear shunters steps have also suffered so they got the similar treatment.
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As can be seen here all go back in place nicely.
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Finally a test run was in order and I am pleased to say that 25 tonner is fully repaired and ready to go back into useful service. Oh you can make out the black cosmetic trunking on the rear of the cab to hide the abuse inflicted with the wire holders
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