Time for an air test with the reverser valve assembled, of course.
Many thinks for your suggestions. They saved a lot of time and thought!
Next remove the rotary slider of the reverser valve. Blow air through each of the four passages.
So here I am blowing through the 4 passages. they are: steam from boiler; exhaust to stack/chimney; feed to outer end of valves; and feed to inner end of valves.
There should be no blockage, but one which is the lead from the boiler. Or the obstacle gets blown out.
With the safety out, there was no problem blowing all 4 - the boiler steam feed blow resulted in all the water in the boiler spraying out, fortunately on the towel. (A lot of white powder came out too - lime, I guess.) Blowing in to the cylinder exhaust vent sounded different from blowing in the steam feed, but it probably should.
So I reassembled the rotary valve and put my air feed in the boiler safety plug. The compressor would get it up to 4 bar before I opened the throttle, and it appeared that air was coming out of both ends of the valve port cylinder/tubes.
Then I put back the valves and checked the timing, put the loco on the rollers and opened the throttle at 4 bar. Still no movement. This is getting weird.
My final test was to leave the compressor running and to turn the wheels, listening to the exhaust beat. I could just distinguish 4 events per revolution, which is correct. They weren't all identical but they seldom are, in my experience.
Moving the piston either way you should not feel much of resistance. If you experience compression
Interesting statement - and true with the valves out. However, on my other locos (except Stanley, which is so worn it will roll downhill on the slightest slope,) they don't roll and you can usually feel a little compression as the pistons move backward and forward. Pushing this loco on the track does not show any resistance at all - pretty much like my Stanley!
If the pistons have no teflon seals, the steam will leak around them and there won't be any movement. Going back to my earlier observation, that the loco spins 3/4 of a turn and stops with on piston halfway - this pic was when it was in steam and stopped - which is most unusual for a steam engine.
So I am left to wonder if that piston is leaking and not providing movement. Shouldn't be a big deal to take the end off and have a look.